The bus was moved 90 degrees again to the other garage bay. The original bus bubble worked well but had the disadvantage of blocking both garage bays. The new-and-improved version only takes up one bay while staying roughly the same size inside. Structure was also added at key points to prevent the sides from sucking in too much when the exhaust fan is turned on.
Bus Bubble v2.0
Primer!
For the first time in this project something new is going onto the bus rather than coming off. (patch metal doesn’t count) Everything inside & out above the trim line was coated with epoxy primer. The epoxy primer creates a barrier between the bare metal and the surfacing layers and topcoats that will follow. Despite careful cleaning and tack cloth usage a good bit of lint/trash ended up embedded in the epoxy. This contamination was caused by the roughness of the bare metal pulling lint off of the cleaning clothes; since the epoxy is smooth this shouldn’t be a problem with the remaining coats.
Bus Bubble Created
Blasting Time
Sandblasting trial run. The rusty front window frames, splash pan, and one of the wheels were blasted with coal slag; initial results were very good. Since the metalwork is nearing an end the plan moving forward is to restore all of the wheels so the bus can be rolled out to the driveway for blasting of detailed areas (non-removable window frames, door jambs, etc.) After that’s completed it can be stripped with a stripping wheel, washed, etched, and primed.